Has anyone had any issues with this gauge mucking with the rail pressure and over all smoothness of the truck? My truck's been acting up. . First I thought it was the TST box, then It did it with the TST harness just on (box unpluged with by-pass, rail harness unpluged) and stock programming...
What would happen is that rail would drop under 5,000 and the idle would float around 500rpm... I took a guess here and pulled it from the harness and the motor idles quieter and the truck is so much smoother.
There's a huge story I could type up here with the different testing and combination.
Just wondering if anyone suspected that gauge for any issues?
What would happen is that rail would drop under 5,000 and the idle would float around 500rpm... I took a guess here and pulled it from the harness and the motor idles quieter and the truck is so much smoother.
There's a huge story I could type up here with the different testing and combination.
Just wondering if anyone suspected that gauge for any issues?