I installed a Quad boost fooler last Saturday. I had seen some good responses on TDR about its effectiveness in lowering EGT's while towing, and for $69 it seemed a worthwhile investment. After installation, the green light was illuminated on the unit, so it looked like it was connected correctly.
I started the truck, and the CEL came on. I took it for a drive, and at WOT max boost pressure would only reach 32psi, and then drop back down to 27psi. Without the Quad, I'd reach 31psi before it dropped to 27psi. I certainly didn't see the 40psi that Quadzilla advertises. The boost response did act differently, but overall it seemed like I had lost some power.
I removed the boost fooler, and cycled the engine on and off a number of times to try and clear the CEL, without success. I was headed out with my FW to go camping, and without the boost fooler installed and the CEL still on, the boost response was the same as when I first plugged the boost fooler in: max boost 32psi, dropping to 27psi. After leaving the truck off for several hours, the CEL finally went out and the boost performance returned to normal.
I would really like to get this thing working, if possible. I filled out Quadzilla's contact form Monday morning, but no response yet. Has anyone had a similar experience, or any ideas as to what might be wrong? Thanks, Scott.
I started the truck, and the CEL came on. I took it for a drive, and at WOT max boost pressure would only reach 32psi, and then drop back down to 27psi. Without the Quad, I'd reach 31psi before it dropped to 27psi. I certainly didn't see the 40psi that Quadzilla advertises. The boost response did act differently, but overall it seemed like I had lost some power.
I removed the boost fooler, and cycled the engine on and off a number of times to try and clear the CEL, without success. I was headed out with my FW to go camping, and without the boost fooler installed and the CEL still on, the boost response was the same as when I first plugged the boost fooler in: max boost 32psi, dropping to 27psi. After leaving the truck off for several hours, the CEL finally went out and the boost performance returned to normal.
I would really like to get this thing working, if possible. I filled out Quadzilla's contact form Monday morning, but no response yet. Has anyone had a similar experience, or any ideas as to what might be wrong? Thanks, Scott.