He's solicited the help of a guy which used to be the Dodge Trans guy at the local dealer. they perfromed an amperage test on the trans circuit. while driving the truck the overdrive solonoid pulled 400mA as did the lock up solonoid. I assume thats the correct reading.
hes going to loop the trans lines to bypass the trans cooler temp valve, not sure why. if that doesn't do anything the trans is finally coming back out.