I changed the fuel filter on Tuesday. .
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So today, I decided to drop the tank, and check out the sock filter. . What a freakin clusterfudge!
Apparently, someone with little clue, much imagination, and no money decided to fix something. Let's see if I can explain it. .
They took the feed and return lines from the sender assembly, then siliconed those connections closed (on the assembly. )
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(I was kinda confused with the Walbro label, however, there's no pump in it. It's merely a float assembly. . )
They then drilled and tapped two 3/8" barbed fittings through the tank's top. One was a 'new' return, and the other was a 'new' feed. Inside the tank, they installed a 'feed' hose from the one barb, down to the bottom of the tank, and installed a small filter. You know, the ones that are about 3/4" diameter, metal, a nipple on one end (inlet) and threaded fitting on the other. And yes, they put it in backwards. Not to mention, a total PITA for servicing.
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I took the filter off, as I saw some junk in it. I started taping it out onto a paper towel, and you would not believe the crap that came out of it.
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So, I went to Advance, and dug through the filters until I found one with 3/8" nipples on each end, as well as a couple feet of fuel line, and some fuel injection clamps. $36. 87 total, including a Gatorade and some beef jerky LOL
For the reinstall, I left the hose inside, lay on the bottom.
Moved the pusher pump from inside the framerail (where it was buried behind the tank) to the outside of the framerail. I added the new inline filter to between the tank and pusher pump, then plumbed it all back together, and reinstalled the tank.
Turned the pusher pump on, turned the key on, bumped the starter, and watched the pressure go to 27-28psi. Started the truck, and the pressure stayed around 24-28psi. . YAY!
Drove it around the block and it stayed above 15, even with a few hard pulls through the gears.
I got back home, and left it run for about 5-8 minutes, and the pressure stayed steady at 22-25psi. With it still running, I turned off the pusher pump, and the pressure slowly dropped to about 3psi. Turned it back on, and it came right back up.
I think my 'new' Airtex is crap, and won't pull enough fuel, or the pusher pump is too much restriction when off. I can test that tomorrow, by removing it from the loop, since it's now outside the rail, and accessible.
I can say, though, that this is a dog, compaired to my '96 p-pumped, #10 plated truck LOL Nowhere near as responsive, either.
Afterward, my neighbor across the street (he's got a 98. 5 24V 5speed) was talking to me about the truck, and I mentioned that my lift pump is possibly dead. So he says "I have a new in-tank assembly with pump and all the parts for the retrofit, including the manifold piece that goes in place of the lift pump. It's in the garage somewhere. If you want it, you can have it, as I've no need for it now. "
I'm like "Sure. "
So anyhoo, I'm gonna tag the truck today, and drive it to work on Friday (6 mi. round trip) and see how it acts. Only thing I have concern with now, is the lethargic acceleration. But again, that could be due to driving the p-pump truck with it's super-responsiveness and tons-o-power LOL