I have an '05 truck with the independent split/dual heating/cooling controls for the driver's side and the passenger's side.
The problem I have is that the passenger side has limited cooling compared to the driver's side (which works great) even though both temperature controls are set to max. cooling. I suspected it might be a blend door and/or actuator problem based on articles I've read concerning 3rd Gen. HVAC issues.
What I've done to date is:
- Had the local Dodge dealership check into it. They recharged the system with freon, replaced a coolant line that had a leaky valve and considered it fixed. The differential cooling problem between driver/passenger side was still there.
- I had another shop address the issue with emphasis on the fact that the AC was cooling well and that it appeared to be a distribution issue on the passenger side. They pulled the dashboard/instrument panel and checked out the HVAC box. They found that all actuators were working properly and scoped the box. It was clear of any blockages or damage. They couldn't figure it out.
I would like to know if anyone has had this problem and know what the fix is or what to investigate further.
Any help or insights would be appreciated. Thank you.
The problem I have is that the passenger side has limited cooling compared to the driver's side (which works great) even though both temperature controls are set to max. cooling. I suspected it might be a blend door and/or actuator problem based on articles I've read concerning 3rd Gen. HVAC issues.
What I've done to date is:
- Had the local Dodge dealership check into it. They recharged the system with freon, replaced a coolant line that had a leaky valve and considered it fixed. The differential cooling problem between driver/passenger side was still there.
- I had another shop address the issue with emphasis on the fact that the AC was cooling well and that it appeared to be a distribution issue on the passenger side. They pulled the dashboard/instrument panel and checked out the HVAC box. They found that all actuators were working properly and scoped the box. It was clear of any blockages or damage. They couldn't figure it out.
I would like to know if anyone has had this problem and know what the fix is or what to investigate further.
Any help or insights would be appreciated. Thank you.