Big Honking Air Filter Installed
First the disclaimer; This worked for me, no claims it'll work for anyone else.
Now that that's out of the way, I'm mildly bombed, and untill last week had tried to make the stock air box work with a stock Fleetguard filter. I just wasn't comfortable with the prospects of pulling oil out of a oiled filter or finding I had one of the rare bad foam filters.
However, with the stock box/filter that had a 2X4"slot cut on the bottom back of the filter housing, and that was connected to a 4. 5 " hole in the cowl duct using dryer vent hose, I was seeing EGT's in the 1300-1400plus range when the truck was working. Boost at these times would be in the high 30's. On a truck only, WOT run, 37lbs. and 1300 plus was the norm.
It should be noted that the Fleetguard filter had been in for 12000 miles, about 9 months. So it wasn't new, but even when new I could pull the filter minder down to almost the bottom with a hard run around the block.
Now for the new filter. Went into the local NAPA store and with the max size filter dimensions in hand, searched the filter catalog and found a filter that works. Here's the filter info;
P/N 2790
style A-159
O. D. 10. 5" X 11. 88" long
Filter medium, pleated paper
$39. 00
This is just a big tractor/truck filter, couldn't determine the recommended applications.
Inlet I. D. is 4" with a app. 1. 5" long lip that accepts the stock turbo connector hose (I fashoned a stiffner insert out of sch. 40 pvc to use in the filter to prevent deforming when the hose clamp is tightened). It has a hard, tough looking black plastic closed end.
I installed as you would the K&N filter used with the Psychotty system.
This filter has dropped my EGT's 300deg. Hard to believe, hense the discaimer above. My first test was a WOT run for about a mile on level road at about 300' elevation. It was 97 deg. with humidity in the 50's. Boost stablized at 20lbs. after spiking up to 38lbs. EGT's spiked at 1200 then dropped to 900 and held for the mile or so I ran the test. With my old system, I would have backed out of the fuel at the 1300deg mark, so who knows what the max EGT would have been. In the past when the gov. had defueled a bit at 2750 rpm and boost and temp stablized I'd have been about 1200degs. on a substained WOT run, (with a empty truck on level ground).
Black smoke has reduced somewhat, and spool up is a little faster.
Again, these results are at about 300' elevation and the filter I'm comparing to was not new. On a stock truck, it would have gone many thousand more miles before a change would have been necessary.
Hopefully if anyone else tries this they will report results.
Also, I don't have the ability to post photo's. But this thing looks great, it's big and fills up the available space. It looks like a truck filter, not some woosy car filter.
First the disclaimer; This worked for me, no claims it'll work for anyone else.
Now that that's out of the way, I'm mildly bombed, and untill last week had tried to make the stock air box work with a stock Fleetguard filter. I just wasn't comfortable with the prospects of pulling oil out of a oiled filter or finding I had one of the rare bad foam filters.
However, with the stock box/filter that had a 2X4"slot cut on the bottom back of the filter housing, and that was connected to a 4. 5 " hole in the cowl duct using dryer vent hose, I was seeing EGT's in the 1300-1400plus range when the truck was working. Boost at these times would be in the high 30's. On a truck only, WOT run, 37lbs. and 1300 plus was the norm.
It should be noted that the Fleetguard filter had been in for 12000 miles, about 9 months. So it wasn't new, but even when new I could pull the filter minder down to almost the bottom with a hard run around the block.
Now for the new filter. Went into the local NAPA store and with the max size filter dimensions in hand, searched the filter catalog and found a filter that works. Here's the filter info;
P/N 2790
style A-159
O. D. 10. 5" X 11. 88" long
Filter medium, pleated paper
$39. 00
This is just a big tractor/truck filter, couldn't determine the recommended applications.
Inlet I. D. is 4" with a app. 1. 5" long lip that accepts the stock turbo connector hose (I fashoned a stiffner insert out of sch. 40 pvc to use in the filter to prevent deforming when the hose clamp is tightened). It has a hard, tough looking black plastic closed end.
I installed as you would the K&N filter used with the Psychotty system.
This filter has dropped my EGT's 300deg. Hard to believe, hense the discaimer above. My first test was a WOT run for about a mile on level road at about 300' elevation. It was 97 deg. with humidity in the 50's. Boost stablized at 20lbs. after spiking up to 38lbs. EGT's spiked at 1200 then dropped to 900 and held for the mile or so I ran the test. With my old system, I would have backed out of the fuel at the 1300deg mark, so who knows what the max EGT would have been. In the past when the gov. had defueled a bit at 2750 rpm and boost and temp stablized I'd have been about 1200degs. on a substained WOT run, (with a empty truck on level ground).
Black smoke has reduced somewhat, and spool up is a little faster.
Again, these results are at about 300' elevation and the filter I'm comparing to was not new. On a stock truck, it would have gone many thousand more miles before a change would have been necessary.
Hopefully if anyone else tries this they will report results.
Also, I don't have the ability to post photo's. But this thing looks great, it's big and fills up the available space. It looks like a truck filter, not some woosy car filter.
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