I think my head let go either while towing, or on the way to get the car I put on the trailer to tow back home. The truck broke down in the middle of the night and in the middle of nowhere (where else?) so I am not sure as to exactly when the headgasket let go.
I was traveling about 75 mpg over flat ground with some slightly rolling swells in the road. EGT was normal in the 750-1000* range before I noticed the strange noise from the engine. I had not had the EGT to above 1200* during the trip. There was nothing unusual happening before the noises started, so I suspect that the damage may have occurred earlier and the added stress and heat buidup in #6 was what started the piston scufffing against the cyclinder walls. It wasnt until I teardown that I discovered the not-too-obviously-blown headgasket, and bits of headgasket material in more than one oil cooling nozzle.
The timing box was a mild one, and the FMS was adjusted for max fueling (63%). Truck is an ETH model, so it ran really good with the setup as I described in the post above. I seldom say EGT values above 1200, and it was really controllable with the right foot. If I really hammered it for a stretch, I could get them to top out at about 1400*.
Since the rebuild, the truck now has total seal rings, new bearings all around, and new seals. I fire ringed the head with the Haisley fire rings, and installed a set of HX35/HT3B twins, and 5" exhaust. I currently have some stock injectors in it until I get the damaged ones replaced (stupid chrylser "mechanic") and the FMS hooked up again. I plan on installing a propane kit for some mild propane injection to see if it does anything for mileage, but have not done that yet. Just have been driving it around for the last couple of weeks to check things out and break it all in. No problems so far.
When the engine was torn down, the piston was not melted really, it just looked scufffed or galled around the edges and skirt. I had to use a hydraulic press to get the wrist pin out of the old piston because it had expanded enough that it was no longer a slip fit into the piston. The rod was not damaged. I can try and post pictures of it on here, but need to get some batteries for the digital camera first. Let me know if you guys want to see it. As a result of the piston scuffing, I honed out the block about . 001 a side (. 002) total on all cylinders to rebalance the bore diameters. The cylinder walls were not really hurt, there was some galled aluminum on 6 and shallow (about . 001 deep or less) scratches on one side. I think it could have been much worse if it had been allowed to run longer after I noticed the noises that didnt sound right.