Help me figure this out.
This is confusing. Many weeks ago I had a fuel leak at what appeared to be the WIF sensor, Replace filter and sensor, plus cleaned up fuel.
Without running truck decided to install my 370's. After installation was testing on back road and power increase was impressive, throttle response was impressive. At 1/4 to 1/2 throttle truck seemed to have more acceleration than with stock 215's plus could hit 40 PSI. WOT just planted you back in the seat, and awsome smoke.
Next day took truck to work some 90 miles away, was giving coworkers rides, truck was running great. On my last blast before entering work we were running the truck hard through the gears. I hit 4th and the truck acted like the clutch was slipping, could swear I smelled burnt clutch. Got the truck back to work all looked OK other than light diesel smell, assumed it was left over fuel from filter. Upon inspection saw more wet diesel fuel But seamed to be at lift pump. Primed the pump and filled my hand with fuel.
Replaced the pump, purge out air and truck starts first try. drove truck for about six hundred miles (over one week), the only thing I noticed was sometimes had to blip the throttle to keep running when first started and what seemed to be a flat spot in second and third applying very light throttle, plus the white smoke. Assumed upstream the lift pump had to be sucking air. Every night I would inspect and tighten anything that looked suspect, and absolutely no fuel leaking. Today I did my first WOT run and truck would not go over 35 PSI and Acceleration was poor and not a ton of black smoke, less than when I had stock 215's.
Tonight I checked to see if I blew a boot off, but that would only explain the 35 PSI boost. Plus I would think black smoke would be worse. Is the problem my timing?
This is confusing. Many weeks ago I had a fuel leak at what appeared to be the WIF sensor, Replace filter and sensor, plus cleaned up fuel.
Without running truck decided to install my 370's. After installation was testing on back road and power increase was impressive, throttle response was impressive. At 1/4 to 1/2 throttle truck seemed to have more acceleration than with stock 215's plus could hit 40 PSI. WOT just planted you back in the seat, and awsome smoke.
Next day took truck to work some 90 miles away, was giving coworkers rides, truck was running great. On my last blast before entering work we were running the truck hard through the gears. I hit 4th and the truck acted like the clutch was slipping, could swear I smelled burnt clutch. Got the truck back to work all looked OK other than light diesel smell, assumed it was left over fuel from filter. Upon inspection saw more wet diesel fuel But seamed to be at lift pump. Primed the pump and filled my hand with fuel.
Replaced the pump, purge out air and truck starts first try. drove truck for about six hundred miles (over one week), the only thing I noticed was sometimes had to blip the throttle to keep running when first started and what seemed to be a flat spot in second and third applying very light throttle, plus the white smoke. Assumed upstream the lift pump had to be sucking air. Every night I would inspect and tighten anything that looked suspect, and absolutely no fuel leaking. Today I did my first WOT run and truck would not go over 35 PSI and Acceleration was poor and not a ton of black smoke, less than when I had stock 215's.
Tonight I checked to see if I blew a boot off, but that would only explain the 35 PSI boost. Plus I would think black smoke would be worse. Is the problem my timing?