Hey guys,
Well my head gasket blew out this morning,the funny thing is that I only have 45# max boost, and only 56,000 miles.
When it went out I wasn't even near max boost,no really I was just minding my own business, driving around drinking coffee.
I talked to some people this morning about it, and they told me that it has happend before 'cause the bolts weren't properly torqued from the getgo.
Good news is that Cummins has one in stock, and I should have it back together by 6pm or so. Bad news is that according to everyone I talked to there not an upgraded gasket for the 24-valve,so I'm stuck with the OEM.
Every thing went smooth when I removed the head,boy that thing is heavy.
The gasket blew out right in the front, just under the wire harness, I'll post some pics of the gasket when I get them developed.
I just have two questions, I'm sure Cummins can tell me, but what is the CORRECT torque on the head gasket? I didn't want to do this today,or fer the next 200,000 miles, so I want to get it right this time.
The other question is,has this happend to anyone else? I mean other than the guys with twins.
One last thing is that every thing else looks good, as far as no carbon buildup, or anything out of the ordinary,as I wouldn't expect it to after 56,000 miles.
Later, Rob
Incase your wondering why I didn't take it to the dealer,well, their just waaaaaay too slow fer me, I need this truck tomorrow,besides all the BOBMING, I didn't even want to chance it.
Well my head gasket blew out this morning,the funny thing is that I only have 45# max boost, and only 56,000 miles.
When it went out I wasn't even near max boost,no really I was just minding my own business, driving around drinking coffee.
I talked to some people this morning about it, and they told me that it has happend before 'cause the bolts weren't properly torqued from the getgo.
Good news is that Cummins has one in stock, and I should have it back together by 6pm or so. Bad news is that according to everyone I talked to there not an upgraded gasket for the 24-valve,so I'm stuck with the OEM.
Every thing went smooth when I removed the head,boy that thing is heavy.
The gasket blew out right in the front, just under the wire harness, I'll post some pics of the gasket when I get them developed.
I just have two questions, I'm sure Cummins can tell me, but what is the CORRECT torque on the head gasket? I didn't want to do this today,or fer the next 200,000 miles, so I want to get it right this time.
The other question is,has this happend to anyone else? I mean other than the guys with twins.

One last thing is that every thing else looks good, as far as no carbon buildup, or anything out of the ordinary,as I wouldn't expect it to after 56,000 miles.
Later, Rob
Incase your wondering why I didn't take it to the dealer,well, their just waaaaaay too slow fer me, I need this truck tomorrow,besides all the BOBMING, I didn't even want to chance it.