Help me out with this one. Took my truck into the local Intermtn. Cummins to have head gasket checked out. I was pretty sure it was faulty after blowing out all the coolant, overheating, etc. while towing a heavy load in the mtns. this weekend.
I'll just post their report: "checked blowby. found engine has 10" of blowby which is the maximum published limit by cummins specs. the elevated blowby could be due to the fact that there is 10psi more boost being fed to the engine than factory spec allows. checked for combustion in coolant. no evidence at this time there are any problems"
I guess I'm still not convinced I don't have a problem... hard to see antifreeze all over the engine compartment and not think somethings wrong. Apparently my engine is fine for stock parameters... but I'm not running stock parameters. I need the truck for towing fairly regularly and am not real enthused by this report - I'm not gonna hit the road with a lot of confidence. I think until I get this figured to my satisfaction I may do the unthinkable and de-tune a little by switching back to the factory boost elbow and limit my boost.
Anybody have any other interpretation of these findings. They didn't seem to impressed by my mods to the truck.
Thanks for any info.
Doug Favor
I'll just post their report: "checked blowby. found engine has 10" of blowby which is the maximum published limit by cummins specs. the elevated blowby could be due to the fact that there is 10psi more boost being fed to the engine than factory spec allows. checked for combustion in coolant. no evidence at this time there are any problems"
I guess I'm still not convinced I don't have a problem... hard to see antifreeze all over the engine compartment and not think somethings wrong. Apparently my engine is fine for stock parameters... but I'm not running stock parameters. I need the truck for towing fairly regularly and am not real enthused by this report - I'm not gonna hit the road with a lot of confidence. I think until I get this figured to my satisfaction I may do the unthinkable and de-tune a little by switching back to the factory boost elbow and limit my boost.
Anybody have any other interpretation of these findings. They didn't seem to impressed by my mods to the truck.
Thanks for any info.
Doug Favor