I finally got a fix on my 10% mileage loss. About 1 1/2 or 2 years ago my mileage went from about 20 to about 17 or 18 mpg. I found a bad KSB solenoid sensor and replaced it. Winter intervened so could not tell if that fixed it or not. Then mileage would be seem to be OK and then go to pot. Finally took it into Cummins Rocky Mountain in Billings and had the valves adjusted and was going to have the injector pump timing checked but the mechanic said usually if it is timed properly it should never go out of time. He then decided to remove the aneroid diaphragm (where the star wheel is and where the air control tube hooks up) to check on the pin down there. The pin was stuck/sticky. He got it freed up and I got the 19 mpg on 1 tank of fuel and it appears to be permanent just looking at the fuel gauge drop versus mileage.
Something else to look for if you have similar symptoms.
Something else to look for if you have similar symptoms.