Something has changed about how my truck runs. Started over a couple months ago. I changed both the engine fuel filter and inline fuel filter and gained noticeable improvement. However, my fuel pedal is very stiff if i try to accelerate moderately to aggressively under low boost, low RPM.
Also, i have more black smoke out the exhaust. Possiibly less smoke right off idle but much more thereafter. In addition, i'm make less boost. I used to feel my ported stock turbo spool around 10 psi, get a little stronger in the mid teens, and really light up over 20 psi. I no longer feel these surges, power still waits to spool but is smoother and seems slightly decreased.
Power is alright, but boost is barely getting into the mid 20s, was previously going to 35 psi. Oh, my cruising EGT is usually high 700s, gauge is erratic, needs repair.
4KGSK makes the engine idle a little choppy after startup until i feather the pedal (i assume it is the GSK). Lift pump and overflow valve have been replaced this spring. I've recently bumped up my idle to over 900 to keep the a/c blowing cold.
My engine has also overheated a few times. Only this past weekend did it actually boil out at a good 270 degrees. I have finally installed a custom fan and Horton clutch which i believe will solve my cooling issues. Could the overheating have affected performance in these other ways? It seems unlikely to me.
Also, i have more black smoke out the exhaust. Possiibly less smoke right off idle but much more thereafter. In addition, i'm make less boost. I used to feel my ported stock turbo spool around 10 psi, get a little stronger in the mid teens, and really light up over 20 psi. I no longer feel these surges, power still waits to spool but is smoother and seems slightly decreased.
Power is alright, but boost is barely getting into the mid 20s, was previously going to 35 psi. Oh, my cruising EGT is usually high 700s, gauge is erratic, needs repair.
4KGSK makes the engine idle a little choppy after startup until i feather the pedal (i assume it is the GSK). Lift pump and overflow valve have been replaced this spring. I've recently bumped up my idle to over 900 to keep the a/c blowing cold.
My engine has also overheated a few times. Only this past weekend did it actually boil out at a good 270 degrees. I have finally installed a custom fan and Horton clutch which i believe will solve my cooling issues. Could the overheating have affected performance in these other ways? It seems unlikely to me.