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anyone have BFG commercial T/A's?

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I dynoed my truck again today and something isn't right. I dynoed in Feb and put down 457/ 1002 on 5/5 and the VA 0n 100%. Today on the same settings it was all it could do to put down 394. 2 and 900 ft/lbs. It would pull real hard to 2000 rpms and fall on its face. Anybody know what is wrong? Ideas?
 
It might be the tires I am running now compared to before (35 BFG M/T's to Toyo M/T's) it is warmer and more humid today though.
 
it was Floor it's dyno. The numbers weren't too far out of line but I am worried as to why it pulls hard to about 2G's and then drops off. I guess the Holley Blue ain't cutting it anymore!
 
rail limiting valve bad maybe? You can plug it off to see if that is it... have not done this but more qualified members will chime in.
 
I changed the FF after we got home and it seemed to help slightly but still falls off, it smokes up to about 2K then clears up. I also checked the rail valve , it seems good since it is not bypassing any fuel with the banjo bolt removed but there is some fuel coming from the return line @ the rail valve( coming from the CP3/injectors)how much fuel is supposed to be returning to the tank? do I have a injector bypassing back to the tank thereby killing my rail pressure?
 
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