This is meant to be informative for others who might experience similiar issues in the future. I recently finished a 7000 mile move from Virginia to Kodiak, AK (via Wisconsin, Oregon, and the ALCAN). I had my slide-in camper on board and was pulling my boat. For the weight police, I was in spec for everything, even axle weights. Total weight 19,000 lbs. All was well until I was ready to depart Astoria, OR for the Alcan and Alaska. Started up the truck (after driving over 4K miles and getting 10 mpg almost exactly at speeds up to 72). Truck was missing badly, but only at idle. I had replaced two injectors 15 months earlier and had 75K on the truck. The symptoms were the same. As I was running heavy I was hoping that carbon would clear up and things would get better. Not so. I have also been running a GDP 2 micron inline in addition to the stock filter. LP fuel read 6. 2 as always. Drove to CA border above Wenatchee and decided to hang 6 new injectors and crossovers since things were getting worse not better. Tried my spare FCA first, no improvement. New injectors in (remans from Cummins NW in spokane). Problems gone UNTIL I took on fuel. Lost rail pressure on the hill leaving Cache CR, BC. Changed both filters and good again. Heard a 'squeal' under hood that went away. Drove to Prince George, filled up same thing happened again. Changed filters, but nervous, now. Went back to Northland Dodge in Prince George and ordered a Rail Relief Valve, figuring that was doing the squealing by letting by and then it was resetting. Had them do diagnostics after talking to their diesel tech (Lee, who is very high speed). Relief was bad. They changed it and checked all the return flows. Issue could not be reproduced. We drove on. Nex morning after leaving the CG, truck lost power again. Changed both filters and all good. Filled up in Ft St. John. Same thing. Change both filters and power came back. Drove to Ft Nelson, filled up and same thing again. Gave up and camped for the night. Found a mechanic shop to drop fuel tank and clean. Little water (had been checking filter and found a little water and misc things, but not much) and a fair amount of dirt, horse hair, and a lily pad looking thing of dirt and sawdust and grime that was floating and plugging the pickup tube. I think it had a specific gravity near Diesel Fuel and only plugged during a full tank. Cleaned up, but now problems getting worse. Put a new injection pump on after the FCA harness gave signal during start cycle that pump was no good. (light flash after 20 seconds of key on). Mostly solved issue. Replaced lift pump with my spare. Pressure went to 8. 3 PSI. Never so good before. Maybe the crud in the pickup had been there a while... who knows. Finally retorqued all injectors/crossover tubes and 6 boat units ($6k) later all is well. Lessons: Can't carry too many filters. Buy good fuel. Have good karma.
A boat unit is $1000 as that is the least amount of money that one can spend to do anything meaningful. Maybe these days it is a truck unit too!!!
I acknowledge that I threw more money at this than I could have gotten by with, but having a leaking injector AND the fuel restriction made this really hard to troubeshoot.
I had replaced the tank with a 56 gallon Xfer flow 18 months earlier and know that all was clean (except I didn't verify the pickup) at that point.
Hope this helps someone else. I would also like to thank Todd West from T&C Diesel who troubleshot this spot on over the phone with me for over two hours of his time... . THANKS!!!!!!
This truck has NO performance mods. I am wondering if I messed up the rail signal by adding an inline rail pressure gauge. Don't know. It is now unplugged.
I had a time schedule to keep as this was a military move and I had a ferry and an airplane schedule to meet to meet my ship which was on deployment.
I am concerned about the robustness of these newer systems and am missing the 12 valve days.
Hope this helps someone on the road fix their problems!!!
A boat unit is $1000 as that is the least amount of money that one can spend to do anything meaningful. Maybe these days it is a truck unit too!!!
I acknowledge that I threw more money at this than I could have gotten by with, but having a leaking injector AND the fuel restriction made this really hard to troubeshoot.
I had replaced the tank with a 56 gallon Xfer flow 18 months earlier and know that all was clean (except I didn't verify the pickup) at that point.
Hope this helps someone else. I would also like to thank Todd West from T&C Diesel who troubleshot this spot on over the phone with me for over two hours of his time... . THANKS!!!!!!
This truck has NO performance mods. I am wondering if I messed up the rail signal by adding an inline rail pressure gauge. Don't know. It is now unplugged.
I had a time schedule to keep as this was a military move and I had a ferry and an airplane schedule to meet to meet my ship which was on deployment.
I am concerned about the robustness of these newer systems and am missing the 12 valve days.
Hope this helps someone on the road fix their problems!!!