I drained the engine oil out of the 91 250 night before last and it did not drain out correctly, after fishing for a bit with a magnet I pulled out a main thrust washer from the crank shaft. I looks to me like the three small tabs attaching the thrust section to the rest of the bearing finally broke and it fell out. The clutch released fine so I think if it was on the flywheel side the upper half is still in place. I have not checked the crank end play yet but will pull the pan hopefully first of the week to inspect damage. It lasted 325,000 miles I priced an underhaul kit from Case IH dealer for $250 does that sound reasonable. I have not called cummins yet but I bet they cannot be much cheeper. If I had another truck in the 300k range I would be looking at replacing the bearings based on my experience fyi. Later Jon