broken Billet intermediate shaft.. what do you think?? also smarty problem!
ok. . so last saturday at left coast diesel's dyno day, i put my truck on the dyno with smarty (tnt) at level 7 with the Torque Management at 3, the Injection Timing at 2, the Rail pressure at 3, and the wastgate off. . the truck did not like the tune for some reason and only hit like 22 psi. . (402hp and 860 tq) so i take the truck off the dyno to see what is going on with it. . i put is on level 5 with the wastgate on (stock) and it was fine. . keep in mind i have never put it above level 5 intil today for the dyno, to be safe. . so then i put it to level 8 with the wastegate still on, but now with the boost fooler on. . to see if it was just the level 7 tune was bad. . and yes for some reason my truck would not run good on level 7. . so i was going to put my truck on the dyno one more time. . so everyone said it will be ok so i put the smarty to level 9 with the Torque Management at 4 (wild), the Injection Timing at 2, the Rail pressure at 4 (wild), the wastgate on (stock) but with the boost fooler on, and the Shift defuel set to off. . i drove it around on the street to see if it was a good tune. . WOW tons of power, so a was at a stop light a put the truck in 4wd and lanched the truck at about 22 psi. . and BOOM!!! and me sayin a F word alot. . and now find out i broke the Billet intermediate shaft clean into two parts. . what do you guy think and comments. . no BS please. .
thanks, chris
ps: keep in mind i have the stock turbo and Injectors. . so i am maybe at the most 450 to 470ish H. P.
#ad
#ad
#ad
#ad
the part of the shaft broken in side the o. d. and the only # i found on the shaft was 5090
__________________
ok. . so last saturday at left coast diesel's dyno day, i put my truck on the dyno with smarty (tnt) at level 7 with the Torque Management at 3, the Injection Timing at 2, the Rail pressure at 3, and the wastgate off. . the truck did not like the tune for some reason and only hit like 22 psi. . (402hp and 860 tq) so i take the truck off the dyno to see what is going on with it. . i put is on level 5 with the wastgate on (stock) and it was fine. . keep in mind i have never put it above level 5 intil today for the dyno, to be safe. . so then i put it to level 8 with the wastegate still on, but now with the boost fooler on. . to see if it was just the level 7 tune was bad. . and yes for some reason my truck would not run good on level 7. . so i was going to put my truck on the dyno one more time. . so everyone said it will be ok so i put the smarty to level 9 with the Torque Management at 4 (wild), the Injection Timing at 2, the Rail pressure at 4 (wild), the wastgate on (stock) but with the boost fooler on, and the Shift defuel set to off. . i drove it around on the street to see if it was a good tune. . WOW tons of power, so a was at a stop light a put the truck in 4wd and lanched the truck at about 22 psi. . and BOOM!!! and me sayin a F word alot. . and now find out i broke the Billet intermediate shaft clean into two parts. . what do you guy think and comments. . no BS please. .
thanks, chris
ps: keep in mind i have the stock turbo and Injectors. . so i am maybe at the most 450 to 470ish H. P.




the part of the shaft broken in side the o. d. and the only # i found on the shaft was 5090
__________________
Last edited: