That was a long day.
I was supposed to have help from a coworker, then he canceled. Short notice I tried to get someone I used to work with at another shop to help, he had plans. Then I tried a buddy of mine, he tweaked his back the night before.
1. Replaced head bolts with ARP studs
2. Installed Jammer 3 injectors.
3. Installed HTT 3pc exhaust manifold.
4. Installed Source Automotive twin kit, including switching out my turbine housing with a divorced wastegate housing on my OEM HX35 (lost an hour dealing with the spring clamp on the compressor housing before I figured out a different route
).
5. Installed 4" exhaust.
After a brief attempt to go home, I had to return to the shop to put on the clamp for the intercooler boot I forgot, and fix an oil leak at the oil filter housing... ssst "OUCH!" (exhaust manifold and turbine housing on top turbo) 1/16 turn... . ssst "OUCH!" 1/16 turn... ssst "GAHHH!" 1/16 turn... (repeat 8 more times).
That was a hard drive home trying to keep the right foot from getting anxious. I was able to keep the boost under 20... barely.
First impressions - I still need to retorque the studs 4 more times before I return to normal driving. Not looking forward to having to pull the intake rockers every time and valve adjust but it's gotta be done.
Boost does spool quicker, obviously, and does seem to be about 3 psi higher than prior at highway speeds.
EGT's down 200* from average driving, but does take longer to return to shutdown temps.
Nice to hear the turbo whine again, but I hate using oil type air filters. Going to find a way to get my BHAF back in.
Still need to get my US gear exhaust brake put back in, and revamp my Water/Meth supply intake with a screen (got gunk in my tank
)
Will update when I get to play.
I was supposed to have help from a coworker, then he canceled. Short notice I tried to get someone I used to work with at another shop to help, he had plans. Then I tried a buddy of mine, he tweaked his back the night before.
1. Replaced head bolts with ARP studs
2. Installed Jammer 3 injectors.
3. Installed HTT 3pc exhaust manifold.
4. Installed Source Automotive twin kit, including switching out my turbine housing with a divorced wastegate housing on my OEM HX35 (lost an hour dealing with the spring clamp on the compressor housing before I figured out a different route

5. Installed 4" exhaust.
After a brief attempt to go home, I had to return to the shop to put on the clamp for the intercooler boot I forgot, and fix an oil leak at the oil filter housing... ssst "OUCH!" (exhaust manifold and turbine housing on top turbo) 1/16 turn... . ssst "OUCH!" 1/16 turn... ssst "GAHHH!" 1/16 turn... (repeat 8 more times).
That was a hard drive home trying to keep the right foot from getting anxious. I was able to keep the boost under 20... barely.
First impressions - I still need to retorque the studs 4 more times before I return to normal driving. Not looking forward to having to pull the intake rockers every time and valve adjust but it's gotta be done.
Boost does spool quicker, obviously, and does seem to be about 3 psi higher than prior at highway speeds.
EGT's down 200* from average driving, but does take longer to return to shutdown temps.
Nice to hear the turbo whine again, but I hate using oil type air filters. Going to find a way to get my BHAF back in.
Still need to get my US gear exhaust brake put back in, and revamp my Water/Meth supply intake with a screen (got gunk in my tank

Will update when I get to play.