rear gears/5Th failure
" UN-true" it has nothing to do with it, Have you read the post that say" don't run 5th " Or i never us 5 th if RPM are below say 1600?? And if you read the owners manual they say don't tow x- weight in 5 th?How many amoung usget to read the owners manual before Purchase?? AND who spends the bucks to buy a vehical with over drive (fuel savings) and Not use it????
About a year ago one member called me ,said he had a 3:54 and only drove to & from work and about once a year took his fishing boat to the lake,cant remember his name ,but Wi. was the state. Lost 5 th at 50 k,also eng was not turned up.
Back in the early -mid 70's the big rigs had the same problem under the IH lable in the tandmen (DANA- IH owned at that time) set-up when cummins went from a 2100 RPM set up- to- high torque/low RPM. 1100-1800 ,only it would shake the nut off the bull gear of the rear-end. The fix in that case was more toque.
Thick shaft & big nut not a problem ,as i recall went from 900-1300 ft lb-had to buy multiplyer. Simple terms more holding power.
With the size of the shaft of the 4500 and the thicknest of the nut more torque is not an option... . They install from the factory with loc-tite so thats out. They started with a loc nut--no help,next came a key-way cut in the shaft and staking one time nut into the keyway-((note my trk i spec'd an ordered in May 96)
got it june 28th) between 1st and 2nd try at a fix(mine had 2nd)
2 days after i owned the rig i found out about the massive failure rate in Elkhart In (towing captial)was testing grounds for cummins (mfg's that owned there own delivery fleet) Now down to one.
My nut came off just past a mounth of owenership (32k) made a quick fix with the OEM worn nut(spinning on a shaft 20 miles) Droped into 4th and fond a shop with a hoist,Dodge ocala,fl said 3 days befor it would get into the door.
Held for 262,000 mi (a year and a couple mo. ,s) Did jump the hp at 135k.
Contacted the Mfg for idea's found they couldnt touch my mileage,got to field test there current fix about to go into production july 98--(This was in june 98)-- failed 49k later reported back,my results were still untouchable,secured a nut used on the shaft with the key cut and did my fix and to date has stayed in place for aprox 400,000 miles.
Another note ,some o/d Mfg'ers state in there add's this wont be a problem if you use one of there units--I ran into a guy broke down on the street in Elkhart with one installed two days after he bought his truck (fuel savings)and his fifth gear went out at 130,oook pulled him to safty and havent heard from him but if he took my advice he has a SB clutch pilot bushing in place and did my simple fix AND it is not a welder... ... ... ... ... ... ... ... ... ... .....
Going to hit print now call if i dont get fix posted tommower morining. Want to see how much of this hits the Mag.