First off, Thanks go out to Jstieger that wrote the thread on tips for installing any of the HTT line of turbos, That helped a bunch
Now then, the install when smooth - Though it would have been nice to have someone help, But it was getting sick of waiting (on a side not, THAT BOOGER (SP66) is heavy!!! and I'm only about 150lbs soakin wet)
Having the tire and wheel well liner out was SOOOOO nice, made the 15mm bolts alot easier to get off...
Now on to the results:
I'll be frank, When I first pulled out and gave a little fuel (after warmed up), I was very unhappy, it was super laggy, and the EGT was stupid high, and the smoke was really heavy, just as heavy as the with the stocker... I was thinking "why, oh why? did I want this thing" --- So I get home and put on the full exhaust (i was running with just the downpipe to go to sears and get a special socket to install the 4th bolt to hold the turbo on. . Yes, I ran with only 3 bolts holding that 38 lbs on the engine (in hind-sight, not the startest thing to do, BUT how else do you get there?) - I think that might be why the first run was terrible, I guess it leaking exh gas out and not spinning the turbo...
After the exhaust was back on, with muffler (thank the lord) - Things went a little different. The spool up was still slow, but only a little worst than stock... WIERD though, the truck felt "peppy"
and no smoke till 12psi, Gotta love the singles program :{ , This turbo needs the TWINS program BAD!! - But after 12psi, it would absolutely rip, BUT the EGTs would still hit 1400 on a run up to 100 mph, I'm like WTF? I though my EGT problem would be almost gone... Well anyway I guess I under estimate the fueling capability of the TST, because this truck was at 105mph, and at redline WAY faster than with the stock turbo... THe dyno will tell it all
BTW - level 5/4 feels about like 6/5 did with the stocker, AND the egts leveled at about 1350* --- We will see after a few weeks if it loosens up
Some pics for your enjoyment:
Now then, the install when smooth - Though it would have been nice to have someone help, But it was getting sick of waiting (on a side not, THAT BOOGER (SP66) is heavy!!! and I'm only about 150lbs soakin wet)
Having the tire and wheel well liner out was SOOOOO nice, made the 15mm bolts alot easier to get off...
Now on to the results:
I'll be frank, When I first pulled out and gave a little fuel (after warmed up), I was very unhappy, it was super laggy, and the EGT was stupid high, and the smoke was really heavy, just as heavy as the with the stocker... I was thinking "why, oh why? did I want this thing" --- So I get home and put on the full exhaust (i was running with just the downpipe to go to sears and get a special socket to install the 4th bolt to hold the turbo on. . Yes, I ran with only 3 bolts holding that 38 lbs on the engine (in hind-sight, not the startest thing to do, BUT how else do you get there?) - I think that might be why the first run was terrible, I guess it leaking exh gas out and not spinning the turbo...
After the exhaust was back on, with muffler (thank the lord) - Things went a little different. The spool up was still slow, but only a little worst than stock... WIERD though, the truck felt "peppy"

BTW - level 5/4 feels about like 6/5 did with the stocker, AND the egts leveled at about 1350* --- We will see after a few weeks if it loosens up
Some pics for your enjoyment:
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