Good Luck !!!!! I also have this problem and have 3 threads going about this , I have a Suncoast tiple disk and There Valve Body also I think there valve body is too much and it leaks fuild into the TC over long sets and when you put it in gear the TC is full and stalls the engine
Ive been allover about this and right this second Im attempting the Fix on the TDR home page ,,, I have the Twisted wire removged from 50% of the split loom its took me about 2 hrs so far and is not looking promising I came here to see if others are removiung the wires all the way to the ECM or what ?
Do a search for Engine Dies By my user name and you will see that I have done many many things to try to fix this problem and it hasnt dont nothing.
Im completly fed up with every thing and I will be Detuning my truck soon back to stock.
Suncoast wants 300 to restall the converter from 1900 to 2100-2200 and they said it may not fix the problem !
Even guyts with Just Shift kited VB have this issue but its not as bad ...
Aslo I think it may be the 5. 0 KDL Do you have the 5. 0 Kick Down Lever also ?????
Theres been many cumminicated fixes for this . .
One was cold Weather reflash of the ECM its been said to work ,,, well it didnt
another is VB pressures to high I had them turned down ,,, Didnt fix it,. ,,
Another was Vp44 is dieing well mine died and new one is in and still didnt fix it .
Ive talked with Jeff Garmon , Dave Gorend and a lot of big time Diesel Performance guys and with there advice Im no closer to fixing the problem than before
It sucks !
Good Luck
And feal free to give me a call aout this issue to anyone on TDR
1-740-819-6661
As this issue has me almost to the point ,,,, no screw that it has me To the point of detune
DM
