Here's some pics of my 12v smoked #6 piston.
Caused by the head gasket material seen below. There was gasket in the #2, 4, 5, and 6 piston cooling nozzles.
Long story short, blew the head gasket with nitrous and too much timing, got it back together, ran for 500 miles until I was chasing a Ford Focus
:-laf . Started knocking, then shaking real bad. Still ran, but was obviously running on 5 cylinders. Get her home, pull the head; son of a %^@#*!
Rebuild time... ...
Now it'll be ready for real fun Oo.
Caused by the head gasket material seen below. There was gasket in the #2, 4, 5, and 6 piston cooling nozzles.
Long story short, blew the head gasket with nitrous and too much timing, got it back together, ran for 500 miles until I was chasing a Ford Focus

Rebuild time... ...
Now it'll be ready for real fun Oo.