Hello, my friend Jamie was sled pulling with his 1997 Dodge Cummins at Fergus fair this weekend. During the pull, his block cracked all alongside the passenger side right through the freeze plugs. Coolant poured out but other than that the engine runs fine.
The mods that were done were as follows: 215 p7100, no plate, . 024 cut delivery valves, ddp 140hp injectors, 64mm Silver Bullet turbo, 3 piece manifold, ported head, arp studs, stock head gasket, marine pistons, studded bottom end.
The Cummins pulls 60+psi boost which is around 600+hp.
We are wondering what could possibly crack this block if its not the notorious ''53 block''.
The mods that were done were as follows: 215 p7100, no plate, . 024 cut delivery valves, ddp 140hp injectors, 64mm Silver Bullet turbo, 3 piece manifold, ported head, arp studs, stock head gasket, marine pistons, studded bottom end.
The Cummins pulls 60+psi boost which is around 600+hp.
We are wondering what could possibly crack this block if its not the notorious ''53 block''.