So I got home last night after work. The truck sat about 45 minutes. I got in and started it up again, fired right up as usual. About ten seconds after it started it sounded like there was an exhaust leak, but from the injection pump side of the engine bay. I shut the truck off, and it dieseled for about 5 seconds at about 400-500 RPMs, and shut off. I waited about 2 minutes and fired it up again. It fired right up, and everything was normal again so I drove off.
Everything seems normal now. The truck doesn't feel low on power, but I do get exceptionally low fuel mileage. I figure something is wrong with the fuel shut-off selenoid or the lift pump, what do you guys think?
Everything seems normal now. The truck doesn't feel low on power, but I do get exceptionally low fuel mileage. I figure something is wrong with the fuel shut-off selenoid or the lift pump, what do you guys think?